TLDR: Oil temp was too high with EXP119 engine. Installed larger 2007X, which failed in flight. So I tried the Aero-Classics 8001652. Read on to learn all the details, but keep in mind that the cooler described in this post was inadequate. See the three other posts below, including the last post where I successfully tried the larger 8001643 with a more deliberately designed duct and oil cooler tray with integrated exit diffuser.
My "larger oil cooler" series:
- Initial larger oil cooler, 2007X.
- Airflow Systems 2007X oil cooler in-flight failure after 75.9 hours.
- Second larger oil cooler, Aero-Classics 8001652, which was inadequate (the post you're reading now).
- Third larger oil cooler, Aero-Classics 8001643, which is satisfactory.
Recall that I increased the size of my cooler from the 2006X to the 2007X since my oil temperature was prohibitively too high in the summer. But why is this my second attempt at a larger cooler? Because my "Airflow Systems oil cooler failed in flight". So for try #2, I decided to use a different manufacturer's oil cooler.
But first, the final result of this second larger oil cooler installation is shown below. Then I'll get into some of the details. For all of the details on why a larger oil cooler was needed, see the post that outlined the first larger cooler's installation.
The image on the left below shows Vans' stock oil cooler duct whilst the image on the right shows the duct I designed.
Now let's get into some of the details on this second larger cooler installation.
I spoke with Aero Classics and opted to try the HE 8001652 (the "HE" is for "high efficiency"), a PMA'd cooler with a core dimension of 6"x6.29" and depth of 3.2" for $1,285. Aero Classic's sentiment was that I should see a 10 - 15% increase in performance over the 2007X. Even if it was 10% - 15% less, I was confident it would be sufficient for my needs. The Aero Classics cooler has 3.5 square inches more cross-sectional area across the core (10% more) and about 3 cubic inches less volume in the core (2.5% less). The Aero Classics engineer also believes their cooler has a better sealing interface to mitigate leakage around the core.
You can read more about the selection of that cooler and a poor-man's comparison of the 8001652 against the failed 2007X cooler towards the bottom of this post.
Here is the HE 8001652 (silver) next to the failed 2007X (gold). Immediately, you can see difference between Airflow Systems' "drawn cup" design on their failed cooler and the "bar and plate" design on the Aero Classics cooler. If the Aero Classics cooler fails, it won't be from a seam ripping open like what happened on the failed Airflow Systems cooler. KitPlanes has a great article about different cooler designs. The fins are very fragile and can be bent with the slightest touch. Keep a toothpick handy to straighten out any fins that get upset. The rows are also wider than the failed 2007X.
Since the HE 8001652 has slightly different dimensions than the failed 2007X, I needed to update my OnShape CAD models for the tray and duct. Here is the model of all three (tray, cooler, duct) stacked together. I ultimately removed the hole on the right support angle in the model in favor of match drilling.
Here's the new tray in place during final fitment. Cost was $61.58 shipped from SendCutSend. I then primed and riveted it together. The image on the left shows initial placement. The image on the right show how I setup to match drill the right support angle: First, a 1.5" angle was fabricated from 0.063" 5052 aluminum and a #12 hole drilled on one side. Next, a 0.058"x0.3125" T6 aluminum was cut to 0.6" to fabricate the spacer. An NAS1149F0363P and NAS1149F0463P washer were place on either side of the spacer. A #12 bit was passed through the hole and twisted enough to score the right support angle so that the hole could be then precisely located and drilled.
Here is the final try in place. I got it (side-to-side) level to 0.4° degrees.
Here is the cooler in place with p-seals adhered. Note that the outflow hose is shown fastened to the engine mount with two Adel clamps. I ultimately removed those to ensure that the hose can offer up its slack when the engine moves during startup and shutdown. You can also see the intake hose coming straight in to the cooler behind an engine mount support. This was a custom length hose I had fabricated to try to mitigate vibration being transmitted into the cooler. I discarded this approach as this hose had no slack to accommodate engine shake on startup and shutdown (see video in this post that shows just how significant this shaking is).
Below is the aluminum duct prior to priming for installation. On my original design for the failed Airflow Systems 2007X cooler, I had the duct printed at 0.0625" thickness with the cooler flange at 0.125". That was overkill and cost $314 shipped last year from CraftCloud. The time around, I had the duct printed for this cooler at 0.04" thickness and 0.0625" at the flange. This was $172.48 shipped, again using CraftCloud.
As I discussed in the post outlining the failure of the Airflow Systems 2007X oil cooler, one of the items I was concerned about was the angle that the intake hose took to come in to the cooler. Vibration from that hose may have exposed a vulnerable part of the "drawn cup" oil cooler design. So I had FF-00020-1 fabricated at an inch shorter ($204.13 shipped from Aircraft Specialty) to account for the new cooler sitting further inboard than the stock cooler position. This would reduce the torquing of the fitting by the hose.
The inflow hose fitting is at 90 degrees pointed forward. As a reminder, always use steel fittings on aluminum to prevent galling (AN822-8), despite what the Van's plans say. Here is what the fittings look like on the cooler (when installed, this would be the inboard side of the cooler).
Here I show the intake hose going in to the cooler.
The outflow hose could be rerouted to come in from the top using a 90 degree elbow fitting clocked at 12 degrees clockwise. With this configuration, the oil cooler won't twist and does not want to translate in any direction when it isn't bolted down. Thus, the outflow hose is perfectly situated.
Here is the aluminum duct in place where you can also see the outflow placement. Again, note that the outflow hose is shown fastened to the engine mount with two Adel clamps, which were ultimately removed.
Final installation shown below. Maybe this coming winter I'll design a carbon fiber transition duct from the baffle so that a straight section of SCEET tubing can be used.
Turns out that this cooler was horribly inadequate, yielding a cruise OilT of 223°F at an OAT of 85°F and a peak OilT of 230°F at an OAT of 86°F in a low power descent! So I dispensed with this cooler and set out on my third attempt at finding a satisfactory cooler. It's worth noting that Aero-Classics would offer me only about $150 in credit to exchange this cooler.
Cost comparisons:
- Cooler: $1,285.00
- Tray: $61.58 + $3.42 (nutplates)
- Duct: $172.48
- Hose: $204.13
- Total: $1,726.61
- Cooler: $940.82 (EA00002/2006X)
- Tray parts: $35.40 (FF-01404A, FF-01404)
- Duct: $135.25 (FF-01406E, FF-01406C)
- Hose: $258.24 (FF-00020-1)
- Total: $1,369.71